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1998 5.7L Vortec Persistent P0305 misfire

42K views 55 replies 15 participants last post by  Roy Allen  
#1 ·
Bought a 1998 K1500 Silverado Z71 with about 167K on her and the first time I had it on the interstate it seemed fine, but the first long hill the SES light started flashing and the whole truck started shaking. P0305 Cylinder 5 misfire. Just thought it was a bad spark plug or something, so not knowing the vehicles history I changed out all the ignition stuff, new rotor button, distributor, wires, and plugs. Re-routed wires for separation. Still starts shuddering at throws P0305 at speeds over 55mph while pulling hills, worse shaking if towing. Mechanic told me it might be a sticking exhaust valve. We've checked valve lift and that was good, valves are very clean for this year, everything good. Checked compression in each cylinder, all 8 reading the same at around 180psi on a brand new gauge. Decided this couldn't be a damaged valve or ring. Pulled intake and found an intake leak, installed new gaskets and sealant to eliminated that as a potential issue. Still threw the P0305 code immediately on test drive. Checked grounds, cleaned, all good. No change. Checked fuel pressure and did a bleed down test, all good there. I had just put a new sending unit, fuel pump and filter on. Cleaned Mass air flow, new air filter, no change. Took a test drive while my mechanic friend watched the scanner and it was retarding the timing advance under acceleration instead of advancing it. Prompted us to replace the knock sensor. That was the first positive change in drivability. The misfire and shaking is less pronounced, it's not knocking drinks out of cupholders anymore, but still throws p0305 on hills. Decided it had to be a bad spider injector. Replaced that last night and it's the newer MFI style, much nicer, and the old one looked pretty fried on cylinder 5 when we removed it. Was confident we found the issue. Nope! Took it down the interstate and while the timing advance and all the numbers on the scanner appeared to be good, the first steep hill and she started to lose power and was popping out of overdrive a lot and then the dreaded P0305 again. I'm just at a loss here. Anyone know what's going on I'm so tired of throwing money and time into this. It's an incredible looking truck for the year I'd love to be able to enjoy it and be able to tow with it occasionally. Right now all it's good for is sub-45mph around town stuff.
 
#27 ·
Probably a stretched timing chain if you couldn't get the distributor to line up like it should using the keyed retainer. If you had to over rotate the distributor something that turns it isn't lined up. Whether it be the cam timing is out or the distributor gear is off or distributor was stabbed wrong. You may want to see if you can get the original distributor to line up on the keyed retainer and be able to hit the + or - 2

If it will and the new one wont. Something is going on there. If neither will then I would suspect the timing chain being stretched.

Still concerned about valve springs too.
 
#28 · (Edited by Moderator)
00pooterSS said:
Probably a stretched timing chain if you couldn't get the distributor to line up like it should using the keyed retainer. If you had to over rotate the distributor something that turns it isn't lined up. Whether it be the cam timing is out or the distributor gear is off or distributor was stabbed wrong. You may want to see if you can get the original distributor to line up on the keyed retainer and be able to hit the + or - 2

If it will and the new one wont. Something is going on there. If neither will then I would suspect the timing chain being stretched.

Still concerned about valve springs too.
I could understand about the valves and I have a set to go in that has a 120 lb closing strength instead of 80 lb. We are just trying one thing at a time before we tear into the engine again. There was a little difference in the way the new one was clocked, either that or the old one was tweaked...We had to rotate the new one a hair it to get it to match. The guy I've been working with is a friend, he was certified up until about 2004. He said he checked a few things and didn't believe it was a timing chain issue.
Yesterday I got a hold of a little bit better scanner and used the OEM advanced function and got several powertrain codes that don't show up on the DTC scan...
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#29 ·
holy crap that's a lot of codes

The only real one i'd be concerned about at this time is possibly the control module codes and the insufficient engine temp code. Does it run cool all the time?

Should run right around 200

The o2 sensor heater codes and cat codes shouldn't affect anything
 
#33 ·
00pooterSS said:
holy crap that's a lot of codes

The only real one i'd be concerned about at this time is possibly the control module codes and the insufficient engine temp code. Does it run cool all the time?

Should run right around 200

The o2 sensor heater codes and cat codes shouldn't affect anything
I have a GM tech2 clone coming. Bound and determined to get to the bottom of it. I have another truck that needs the ABs bleed capability so I just went ahead and bought the scanner, and if it ends up being the PCM I can reflash the new one with it. However, looks like a wiring or ground issue could cause these 601-604 codes so we are going to run through those first.
 
#35 ·
Just to update after a while trying different things. The computer swap went well without a hitch. reprogramming successful but no change in performance the miss is still there and getting worse it seems...cruise control wont even stay engaged on the interstate now. New coil and ignition module seemed to make things even worse. I've already had to replace those with a third so it actually starts good. Want to drive it off a cliff.
 
#38 ·
I have a customer with the exact issue you are facing. He likes to do his own work and I told him to check for broken springs. His misfire code sets a P0303, but at 2500 RPM in neutral it shows misfires on #5.

I'll update you when he gives me feedback.
 
#39 ·
justins1998 said:
I haven't been able to. I'll have to hire a mechanic I think my friend is tired of working on this truck with me. lol
They're fairly easy. A basic spring compressor from autozone will do the job. Valve covers are easy to pull.

Just need to fill the cylinder with air or string to keep the valves from falling down while pulling the springs.
 
#41 ·
Son of a gun. Thank you for updating the post.

I thought that was a 99+ thing.

Noted, and seriously thank you for updating the post.
 
#44 ·
Stop throwing parts at them guys and just have the heads rebuilt. It DID fix my truck finally and I should have started there and not wasted the extra dough. Although not an easy job to shade tree, and expensive at the shop, I think this is the root cause of many "mysterious" misfires you can't fix with electronic parts. Dirty, sticky valves will not be helped much if at all by seafoam and treatments etc... and driving the piss out of it only made it worse cause it got hot.
 
#47 ·
I didn't rebuild my heads, mechanics said there wasn't a reason to except maybe to clean all the carbon and gunk off them and remove carbon from the combustion chamber. Try a water de-carbon, look it up before trying and use the Seam foam oil/fuel treatment in the crank case, pour the rest in the gas tank and drive it for 300-500km, then do an oil change. Makes a hell of difference
 
#48 ·
I am having the exact same problem with my 1998 Silverado with 214k miles. I have been fighting this for two years. New plugs, wires, cap, rotor, MAS, MAP, spider injector, all AC Delco parts, good compression and still starts running terrible at 70 in OD. Shakes to high heaven and if you stay on it will eventually die and stall. Will start right back up. I have tried sea foam and seemed to help a little. Will set a 306 miss fire or 300 miss fire, has set a MAP and MAS codes in the past. Runs great until you get to around 65 and it goes into OD and the faster you go the worse it gets. I think I will load it up with a big charge of seafoam and give that another shot, then consider head work.
 
#51 ·
Just letting anyone that's interested know, I had my lifters replaced and that helped the truck gain a ton of lost power but still had the misfires/shaking at highway speeds but just faintly.
I asked the mechanic what he thought it was and he had no idea. Asked him what it tested for fuel pressure and he said 53psi..... From reading on these forums its pretty well known that 60psi is the bare minimum for these trucks or they run like crap. Replaced the pump and problem is 100% fixed. Ran a full can of intake sea-foam to help clean out cylinder #3 as it apparently has had a collapsed lifter for over 4 years and other weak lifters that 6 plus other mechanics couldn't troubleshoot... Anywayssss, ran a whole can down the intake and took it for a good drive, smoked like a son bitch, ran noticeably better. Just to be safe put two cans of sea foam with a fresh full tank of gas, put 150ml in the crank case to help clean up all the carbon build up from weak lifters, a week later and the truck continues to perform even better. No more losing O/D from engine limping itself along and no more shakes on the highway, even with 2500lbs on my trailer.

Thanks for everyone who helped, cant always trust a mechanic to figure it out but it helps to have a good one on your side, good luck to the rest of you p0300 chasers
 
#53 ·
Just so you know, the problems fixed. So you can stop posting random vids
 
#54 ·
I am working on a friends 1999 Silverado K1500 160,000 miles on it, Misfires on cylinder #3. He has gone though all the steps many of you have reported. New Spider, Wires, Plugs, Cap, Rotor and much more. Still had #3 misfire. He loves this truck, has put a ton of money into it, new Paint, new front end rebuild. If it needed it he did it. He kept going back to shops trying to fix this misfire. He dumped thousands of dollars into it before he called me for help. I am not an expert but have 40 years in the industry, I was ASE certified in Engine Repair , Engine Performance and all 5 areas of Engine Machine so GOLD certified ASE but with no prior Vortec experience except for one truck, I come to the forum to see what I should know before working on a set up I do not know.

He supplied paperwork showing this truck had recently had a compression check on #3 and it had 165 PSI so I did not double check that. I did determine that the lower intake manifold was leaking a tiny bit of coolant and had a slight vacuum leak right at the #1 and #3 hold down bolts. I pulled the intake, the gasket was broken at the front from being over torqued by one of the shops he paid dearly, but he has been chasing the #3 miss since 2019. With the lower manifold gasket repaired, upper manifold gaskets replaced and checked for straightness the engine fired up beautifully, zero misfires on any cylinder. Fuel Trims were adjusting back to normal within 5% and getting better. Ran it for a good hour. On initial Test drive it feels great, transmission shifting really smooth and then bang, #3 misfires come back and it forms a dead miss on #3.
When we got home I went back to basics, took my own compression check, Leak Down Test, found near zero compression #3, leak down was over 90% leak at 100 PSI. ????? I know this cylinder was running perfectly just 30 minutes ago? Took a vacuum check and it had 18.5 inches at idle with one dead cylinder. That seemed impossible to me. I Pulled the valve cover, with the leak down tester hooked up and pushing 100PSI into #3, Rocker arms removed I still had 90% or more leak on 3. I took a pry bar and pulled up the exhaust valve because my leak was into the exhaust and not the intake. By pulling up on the #3 exhaust valve the cylinder sealed up and my leak down was now only 5%. If I tapped on the exhaust valve with a ball pen hammer the leak down jumps back up to more than 90% leak and the valve does not snap closed after the tap. With the exhaust valve pried up a little and the leak reduced to under 5% I could tap the intake and hear the valve snap closed after each tap. With 100 PSI in the cylinder the valve springs are no longer in play, the air pressure will hold the valves firmly in place.

I did some GM bulletin checks and GM claims the valve spring issues they had did not start till 2002 and ran through 2007 I think? 1999 did not come up for valve spring failures.

Pulled both heads, really stunk having to do this 2 days after removing the intake manifold for the gasket repair. The sticking exhaust valve did have carbon build up on the stem keeping it from closing. I think the Build up has just been getting worse since 2019 when the misfires started, truck only goes 2-3,000 miles a year. Driver never pushes it to blow out the exhaust he pampers it everywhere he drives.

A buddy owns the machine shop I use, we have been friends 40 years and I trust his opinion completely. He says he can't count all the vortec engines he has fixed for random misfires caused by the sticky exhaust valves. It just slowly builds up till it becomes a factor. My guess as to the cause would be a little oil getting past the valve stem seal and burning to the surface of the hot valve caused the build up.
When the valve sticks open you have a dead miss, when it starts moving again you might have a perfectly good running engine making this issue very hard to find.

In my buddy's case initially it only happened while pulling his trailer over a long hill, then it slowly progressed till it was happening as soon as the engine hit full temperature. We have the Heads in being rebuilt right now, won't have them back till late next week but I am 100% sure this is the problem.

Maybe the Sea Foam treatment could have cleaned up the valve stems but I really doubt it, the build up on the valve stems felt rock hard to me.

I did advise my buddy to Drive it Like You Stole it once in a while to blow out the carbon. He laughed and said he will try. I think all the low RPM putting around did not help him keep the valves clean.

Hope this helps another owner get fixed up.


June 1, 2025 UPDATE:
Follow up from my Feb 24 post. The 99 Vortec Silverado engine is still running perfectly after the valve job. It was a carbon build up issue on the valves causing it to hang the valve open. That one is fixed!
 
#55 ·
I have a 1998 GMC Sierra K1500 5.7L Vortec with 272,000 miles on it. I love my truck. I have gone around and around on this "misfire under load" for many years. Finally, I checked the timing chain by removing the distributor cap and slightly moving the crankshaft back and forth a little bit. When you move the crankshaft you should see IMMEDIATE movement of the rotor on the distributor. In my case, I could move the crank probably 2-3 degrees before the rotor moved. So, I went after the timing chain and gears. Not a really tough job, just took a few hours to do. When I got to it there was a LOT of slack in the timing chain. Probably 1/2 to 3/4" of play side to side. I bought the truck with 18,000 miles on it. I never replaced the timing gears and chain in all those 24 years or so. So, I replaced the gears and chain and voila! First drive...NO MORE MISS under load. Timing chain and gears! I hope this helps someone.